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Here are the steps I follow to reproduce the issue:
1. compile 5axis kinematics
2. run configuration
3. home all axis
4. move machine a little bit not to get joint limit errors
5. move B axis in “+” direction works fine
6. move B axis in “-” direction – silent stop, no error, just machine power is toggled automatically
This is what I expected to happen:
move in B- direction
This is what happened instead:
machine power is toggled, no error message, nothing
It worked properly before this:
before upgrading to 2.8.0-pre1 from 2.7.8
Information about my hardware and software:
* I am using this Linux distribution and version (often, shown by lsb_release -a): Debian/Wheezy
* I am using this kernel version (shown by uname -a):3.4.9ßrtaiß686ßpae
* I am running …
* A binary version from linuxcnc.org (including buildbot.linuxcnc.org)
* I am using this LinuxCNC version (shown in package manager or, for git versions, scripts/get-version-from-git):2.8.0-pre1-2944
* I am using this user interface (GUI) (e.g., AXIS, Touchy, gmoccapy, etc):Axis
* I am using this interface hardware vendor and chipset (e.g., parallel port, ethernet port, FPGA card): parallel port